Dec
22

Vroom, Vroom

By Steven · Comments (1)

Got her up and run­ning again this morn­ing to check what I thought was a minor exhaust man­i­fold leak, and it turns out that we do have one, not from the man­i­fold itself, but because we neglected to install the man­i­fold heat tube that goes up to the choke assem­bly.  I ran her for a solid 30 min­utes and every­thing checks out just fine.  As noted ear­lier, we do have a prob­lem with the gen­er­a­tor mak­ing a racket and not charg­ing.  Every­thing seems to be solid and tight, with no leaks, oil that is, my newly built radi­a­tor is leaking.…eeekkk.  In fair­ness, it is very minor and while I can­not locate the source, it is com­ing from the lower left cor­ner, there are no fit­tings or hoses in the area so I sus­pect a pin­hole in the sol­der joint attach­ing the lower tank to the core.  So it will have to come out and go back to the shop for pres­sure test­ing and repair.

Exclud­ing the radi­a­tor, and gen­er­a­tor the only other issue I have is a baf­fling sit­u­a­tion with the dis­trib­u­tor again.  I set the tim­ing per­fectly, tighten it down and within min­utes it backs off and dis­rupts the tim­ing to the point where she stalls.  Right now, the only way I can keep her run­ning is to put a wood block between the intake man­i­fold and the vac­uum advance on the dis­trib­u­tor to keep it from turn­ing back.  When the dis­trib­u­tor is out, the shaft turns freely with no resis­tance so I guess I have no choice but to pull it out and dis­as­sem­ble it com­pletely, some­thing is bind­ing up and caus­ing the whole assem­bly to turn even with the hold-down wrenched down tightly.  I have no clue right now.…

After some seri­ous thought and because our goal is to have a reli­able daily dri­ver I’ve decided to scrap the gen­er­a­tor and volt­age reg­u­la­tor in favor of a one wire Delco 10 si alter­na­tor rated at 63 amps.  When I picked up the car, there were at least 4 new and used volt­age reg­u­la­tors in the trunk indi­cat­ing a con­stant and chronic issue with the sys­tem and frankly I want to enjoy the car and not keep tin­ker­ing with it when it is done.  I will how­ever have the orig­i­nal gen set rebuilt and put it on the shelf, should I decide to put it back in later.  This set-up should sup­ply plenty of juice to keep every­thing run­ning and fully charged even with long peri­ods of idle.

While run­ning the car today and with it up on jack­stands we ran the whole dri­ve­train for quite some time.  Every­thing checks out nice, with no noises or vibra­tions from the tranny, dri­ve­shaft or rear end, either in for­ward or reverse.  No exhaust rat­tles, leaks or issues of any kind

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All of the hard work came together this morn­ing when I once again pulled the dis­trib­u­tor and cor­rected its instal­la­tion, re-installed the plugs, changed her oil, gave her a shot of start­ing fluid and BOOM off she went sput­ter­ing and snort­ing, pop­ping, and back­fir­ing.  Nat­u­rally after sleep­ing for decades no one expected her to awaken with a smile, but she is awake.  Admit­tedly, I shut her down after about 20 sec­onds amidst the unex­pected noise.

I made some minor car­bu­re­tor and tim­ing adjust­ments, started again and she smoothed out dra­mat­i­cally but there are some weird and scary noises com­ing from the front end, so I shut her back down again.  I didn’t think any of the noises were com­ing from the engine itself so I removed the power steer­ing and gen­er­a­tor belts, re-started and the noises were now gone indi­cat­ing pos­si­ble bear­ing issues in either the gen­er­a­tor or power steer­ing pump.  Again, I shut her back down, because with­out the belts the water pump was not turn­ing and I was not going to take a chance of her overheating.

I put the power steer­ing pump belt back on, re-started again and this time she ran qui­etly at a fast idle for about 20 min­utes until she came up to nor­mal oper­at­ing tem­per­a­ture.  Seems like the noise was com­ing from the gen­er­a­tor and I will have to check it out later.  She ran smooth, solid and with­out so much as a hic­cup and over­all I’m just tick­led pink.…. Note to Santa, you can skip my house this year, today was good enough for me and besides I really have not been all that good anyway…lol.

After shut­down a com­plete inspec­tion showed a minor oil leak at the oil fil­ter result­ing from a loose com­pres­sion fit­ting and there is an issue with the dis­trib­u­tor hold down allow­ing the tim­ing to back off as the motor is run­ning.  All minor and eas­ily fixed.  I will try to post video of the start-up when I get a minute, but it is get­ting crazy with the hol­i­days almost here.

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Well we really did not do bet­ter this week.… I’m really pressed for time and have to fin­ish the rental unit so the ten­ant can move in for the New Year.  With that, the Hol­i­days and every­thing else com­ing together at once I really don’t have the time to prop­erly work my way through the start-up problem.

We have spark, fuel and com­pres­sion but still no go.  I stopped by Spring­field Auto Machine to pick their brain as I was stumped.  The guys there are really great and after some dis­cus­sion the con­sen­sus seems to be that the engine is prob­a­bly 180 degrees out of time.  All the while I’m think­ing, how the hell can it be out of time, I fol­lowed the man­ual explic­itly.  Brought the motor to TDC and installed the dis­trib­u­tor every­thing was per­fect until Dick asked me what the valve posi­tion was, it was about this time that the “light bulb” went on in my head and I’m think­ing “Holy Crap” I installed the dis­trib­u­tor on the exhaust stroke, not the com­pres­sion stroke.….. Dick and Brian were very patient and in fact did not even roll their eyes… they even offered to come to the shop and get it started for me.  I stopped to see them on my way out of town and for the rest of the trip sit­ting in the car I was rolling this stu­pid sit­u­a­tion around in my head.  Once back in town I could not stand it any longer, cleared my sched­ule, went over to the shop and once again checked every­thing.  Sure enough, when I brought it up to TDC on the com­pres­sion stroke and checked the dis­trib­u­tor it was point­ing 180 degrees in the wrong direction.….……

I could have put the plugs back in and attempted to start, but with all of the screw­ing around and the major flood­ing of the engine in our many pre­vi­ous attempts the oil smells like gas, not to men­tion the fact that we prob­a­bly pushed a ton of fuel into the exhaust.  So we are going to change the oil and let it sit for a while to dry out before try­ing to start, prob­a­bly this weekend…

I promised my wife I’d take a break from every­thing so we are off to the Mohe­gan Sun Casino for an overnight trip to see the Boston Pops and prob­a­bly have a dozen cock­tails while I stew about how dumb I really am.  I’m not sure this trip is a great idea with the way my luck is run­ning…  I have had that dis­trib­u­tor in and out of the car at least six times and I can­not believe that in all those attempts “blind luck” would not have allowed me to get it in the right way just once!!!  Geez…That would be like flip­ping a coin six times and com­ing up heads every time, with luck like that maybe I should’nt be gam­bling at all.

We’ll be back at it and try again this weekend.

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Dec
06

Caddy Update

By Steven · Comments (0)

Time con­straints have just been insane, what with putting up the tree and dec­o­rat­ing the house, along with try­ing to get the rental unit ready for the end of the month.  Oh yeah, I also have to work for a liv­ing.…. Unfor­tu­nately, the “Gray Lady” has had to play sec­ond, third and even fourth fid­dle recently, but when time allowed I have been play­ing around a little.

My major prob­lem at this point is that I am get­ting no spark, so she won’t start.  I installed a Pertronix Igniter elec­tronic sys­tem under the cap think­ing I was doing a good thing, but what looks like a sim­ple instal­la­tion has been a real PITA.  First, the dis­trib­u­tor had to go out to have the slop taken out of the shaft, then with the new parts installed we had no spark, so I messed with it for a cou­ple hours, took it back out and after talk­ing to CB Per­for­mance, they walked me through bench test­ing the unit, which checked out OK.  Re-installed it and still no spark, appar­ently a ground­ing prob­lem, took it back out and cor­rected the ground.  Re-installed again, and still no spark, so now we swapped out the new coil think­ing it might be bad.… No Dice, still no spark.  So now the dis­trib­u­tor comes out once again, this time when I bench test it, it fails, so it has to be sent back for replacement.

It seems Murphy’s Law is work­ing over­time with this one and I am tired of wait­ing, so the points and con­denser will be going back in, so we can get her started.  I am about as frus­trated as I can be at this point.  With no other projects ready I began strip­ping the trim from the rear sec­tion of the car.  The tail light bezels, chrome trim on the fins, the Cadil­lac let­ters on the fins, trunk vee and emblem are now off the car and will be sent off for plat­ing and anodiz­ing, then put away to be re-installed once she is painted (hope­fully, next Spring).

It has really been an aggra­vat­ing and stress­ful week, hope­fully the com­ing week will show bet­ter results.…Till then..

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Nov
30

Baby Steps

By Steven · Comments (0)

I re-installed the fuel tank today with the new fit­tings, and it is finally sealed.  I put about 12 gal­lons of fuel in and every­thing is tight with no leaks.  Mov­ing on, I tem­porar­ily installed the bat­tery tray, put in a new bat­tery, con­nected all of the cables and pow­ered up all of the elec­tri­cal sys­tems which thank­fully appear to be oper­at­ing correctly.

I installed the new plug wire set, con­nected every­thing and the only thing left is to install the spark plugs.  Next step was to crank her over to prime the fuel sys­tem.  What I thought would take a cou­ple of min­utes of crank­ing took only about 45 sec­onds to get the fuel from the tank to the carb.  Unfor­tu­nately it was at this point that today’s prob­lem reared its ugly head.…..

With the fuel sys­tem pres­sur­ized the fuel fil­ter is leak­ing like a sieve.  Pre­vi­ously, I had taken the time to dis­as­sem­ble the glass bowl fil­ter, clean it and the ceramic fil­ter ele­ment and put it back in, but appar­ently the gas­ket is dried out and not mak­ing a proper seal, so had to call it a day.  With fuel sprayed on the top of the motor I was tak­ing no chances that a spark would light the beast on fire.

At this point, I need to either re-gasket the old fil­ter (the method I pre­fer) or scrap it and just install an in-line fil­ter between the fuel pump and the carb, either way will require me to remove and re-install that fuel line.  I will do a lit­tle leg work tomor­row to fig­ure it out.  If I can find some nitrile rub­ber stock I will just make my own gas­ket, if not, I’ll just have to punt.  We are about 1″ from start-up, while I can’t wait to hear her run, I need to make sure every­thing is per­fect before doing so, tomor­row is another day.

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Nov
28

Yikes.…

By Steven · Comments (0)

With visions of hear­ing her finally roar to life Paul and I came in this morn­ing, put 6 gal­lons of fuel in the tank and got busy check­ing minor details and then I smelled gas fumes.  The fuel tank was leak­ing at the con­nec­tion to the fuel line.  What we thought would be just a loose line con­nec­tion took the rest of the day with­out a good res­o­lu­tion.  So no start up today…

I can’t be sure, but I think there is a fit­ting miss­ing from the tank itself.  Much ear­lier we installed a new stain­less steel fuel line and it seemed to fit per­fectly into the tank.  The prob­lem seems to be that when the nut on the line is turned down into the fit­ting, the head of the nut shoul­ders on to the tank before a good com­pres­sion seal can be made allow­ing a very small leak that drips fuel.  We spent hours try­ing to solve this issue.….

At first I thought the flare on the new line had been dam­aged, so we re-flared it and tried again to no avail, with the tank in the car it is hard to really see what is hap­pen­ing.  We tried installing new and dif­fer­ent fit­tings and all of them seemed to have the same prob­lem, they would shoul­der on the tank before mak­ing a seal.  With no other options, we took the tank back out of the car and I still can­not get over the fact that the tank drain is not on the low­est point.  There is no way to com­pletely drain the tank by pulling the plug which is a bout 2 inches above the bottom.

Once out we are able to bet­ter visu­ally inspect the tank fit­ting. Gas Tank Fitting It seems that it is not a com­pres­sion fit­ting at all, what we see is a fit­ting that has a pipe flared on one end inserted into the bot­tom of the tank to pick up the fuel from the bot­tom, so we are attempt­ing to mate two flared pipe ends together.  What I need is a fit­ting with a bul­let tip that is tub­ing thread that can insert into the tank fit­ting and com­press the flared pipe that is in there seal­ing it and then find a way to go from that fit­ting to a stan­dard 5/16″ com­pres­sion fit­ting so that the fuel line can attach to that.  If these fit­tings are not avail­able, the only other solu­tion will be to take the tank to some­one to have a new mod­ern fit­ting either welded or sol­dered into the tank.….

On the way home I stopped in at NAPA and Lonny and I spent 30 min­utes try­ing to resolve the issue going through box after box of fit­tings.  We finally found what may be a work­able solu­tion.  These guys at NAPA really rock, when I went to pay him, he told me to “have a nice day” and would not take any money.  The only bright spot to a really crappy day.

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Nov
27

Burp.……

By Steven · Comments (0)

I’m back to work on the “Gray Lady” after a ten day break.  Other than a few min­utes here and there most of my time has been involved in try­ing to re-hab a rental unit and get it ready for Decem­ber 1st.  Unfor­tu­nately, after 12 gal­lons of paint I am still not fin­ished (with 1 room left to go) and the floor­ing contractor’s can­not get there until Decem­ber 2, too much left to do and to lit­tle time to do it so the dead­line has been moved to Jan­u­ary 1st.  That being said, I put the paint brush aside and went back to the car with the hope that I could get her started this weekend.

While on hia­tus my needed parts arrived.  The new gas cap arrived from Baily’s Garage, and Cadil­lac Inter­na­tional was very good about hav­ing a new pipe bent to replace the left rear inter­me­di­ate pipe that would not fit on our last go round and finally CB Per­for­mance shipped the dis­trib­u­tor kit with a new flamethrower coil that had been back-ordered for the last 2 weeks.

Paul had the day off and came in to give me a hand, while he was fin­ish­ing up the exhaust, I worked on the dis­trib­u­tor con­ver­sion to elim­i­nate the points and install the elec­tronic mod­ule under the cap. Distributor The kit fit per­fectly, but there was a prob­lem with some slop in the shaft that allowed it to float up and down to much.  The kit requires tol­er­ances of no less that .010 to no more than .060 between the sen­sor and the mag­net plate under the rotor.  My friends down at NAPA auto parts helped me to solve the prob­lem by grind­ing out the pin hold­ing the gear, pulling the shaft, inspect­ing the bush­ings and then installing 2 shim wash­ers between the top of the gear and the bot­tom of the shaft tube.  Now it is per­fect with a con­sis­tent tol­er­ance of .030 and no slop so I installed it on the engine.

With that piece of the puz­zle fin­ished, the last item we need to con­nect is the tranny cool­ing lines.  Ear­lier and with great dif­fi­culty we had installed them, guess­ing at their proper loca­tion and it turns out we guessed wrong.  Think­ing back, it would have been smarter to install them before we hoisted the engine back in place, but we live and learn.  Not sure about the loca­tion, I went back to the ref­er­ence pho­tos I took when tak­ing every­thing apart, armed with this new info, we took them back out and re-installed them in the cor­rect posi­tion. Tranny Hose Then I made up two new rub­ber lines to con­nect the tranny set to the the lines com­ing from the radi­a­tor itself.  Stick a fork in us, we are done, all sys­tems are closed, oil is in, tranny fluid filled, power steer­ing fluid in, coolant in and we are nearly ready to start her up, hope­fully tomorrow.

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Nov
26

Happy Thanksgiving.…

By Steven · Comments (0)

Mary Lee and I wish all a very happy and  safe Thanks­giv­ing Holiday.…..

screenshot062We thought about cook­ing the bird on the exhaust man­i­fold while cruis­ing, but unfor­tu­nately we are not yet run­ning (this week­end is the tar­get), so we decided to send the bird to the beach instead.….

As you cel­e­brate with fam­ily and friends, take a moment to thank all and pray for those who can­not be with their fam­i­lies today because they are pro­tect­ing our right to do so.

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Nov
15

Exhaust Issues Continued

By Steven · Comments (0)

We began from the man­i­fold on the driver’s side (now that the man­i­fold issue has been cor­rected) to the muf­fler, then through the x part of the frame.  All the while rebuild­ing the hang­ers as we went, all is well to a point.  Now with the last large piece that goes up and over the rear axle (allow­ing the axle to float) on its way to the res­onator we again have a prob­lem.  I can only assume that the piece is bent incor­rectly, the large U-shape bend is closed to much allow­ing the pipe to rub the rear wheel and poten­tially also hit the lower mount for the shock.  The parts are not inter-changeable so I am con­fi­dent we have every­thing in the right place and when we loose fit the sys­tem we did not see the prob­lem.  We are in the cor­rect place above the axle, but in the wrong place below it.

With it being Sun­day there is not much else we can do.  I don’t have a pipe ben­der and I’m pretty sure if I try to open up that bend with­out one I will kink the pipe and restrict it.  I will try to cor­rect it next week and if I am not able to open it up, I will have to talk to them over at Cadil­lac Inter­na­tional about a replace­ment.  We are 16 man hours into the exhaust and still not completed.

We installed the radi­a­tor sup­port frame, the new radi­a­tor, hoses and heater core lines along with a new ther­mo­stat.  I wanted to be able to start-up with­out the fend­ers on so that we would have more room to work on any adjust­ments and be able to send the car out for an align­ment before we close every­thing in.New Brackets  How­ever, that sup­port frame is attached with only one bolt at the base and kind of floats there, it is actu­ally the fend­ers and splash pan­els that sta­bi­lize it and now I am wor­ried about try­ing to start-up with it not secured, there is not a lot of clear­ance between the radi­a­tor and cool­ing fan.  I decided to fab­ri­cate two tem­po­rary sup­ports that run from the sup­port frame to the front of the frame where the bumper brack­ets mount.…. Prob­lem solved and we are good to go now.

Now another prob­lem, with the radi­a­tor up, we can see that the tranny cool­ing lines are in the wrong place.  They will have to be pulled out  re-routed and re-installed cor­rectly so that they will meet up with the front set that goes through the radi­a­tor sup­port frame.  Once that is done, we will install 2 new hoses to con­nect the two orig­i­nal metal tubes, and will fab­ri­cate them in the shop to close that part of the sys­tem.  The only things keep­ing us from start-up now are the com­ple­tion of the exhaust sys­tem and instal­la­tion of the dis­trib­u­tor and coil (we are wait­ing on parts for those).

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Nov
14

Exhaust Issues

By Steven · Comments (0)

We began assem­bly and instal­la­tion down the pas­sen­ger side of the vehi­cle now that we have the flanges.  We took a con­sid­er­able amount of time mak­ing sure every­thing was just per­fect.  As we got to every hanger, we pulled it down cleaned the metal parts and installed new rub­ber that we cus­tom made in the shop using the old ones as pat­terns.  The only dif­fer­ence between the orig­i­nals and ours is they were riv­eted together and instead are now bolted.  The sys­tem ordered from Cadil­lac Inter­na­tional appears to be of very high qual­ity and every junc­tion lines up at a hanger just as it is sup­posed to.  The pas­sen­ger side is now com­plete and rock solid.  Amaz­ing factoid.…it took 9 muf­fler clamps to assem­ble just that one side, from the man­i­fold to the muf­fler, to the res­onator and then out to the tailpipe.

Now for the driver’s side, the real fun begins.….. Here we have not only the exhaust flange but the heat con­trol diverter valve, plus 2 gas­kets.  Well it seems the new flanges are much thicker than the orig­i­nals and now the man­i­fold studs are not long enough to get the nuts to grab.  No way around it, the studs have to come out and be replaced. Engine Right The first one came out easy as  pie and we then spent an hour try­ing to remove the sec­ond one (Murphy’s Law strikes again!).  We finally decided the only way to get it out was going to be to remove the man­i­fold (and ruin the new gas­kets),  I was sure we were going to break it off and have to send the man­i­fold out to be drilled and tapped.  Once on the bench in a vise and with a pipe wrench it finally gave way and came out.  New studs are in and the man­i­fold is re-installed and finally we are ready to go.  Time to call it a day.

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